Re: Widerøe hendelse i Svolvær i 2010
Aviation Herald har gjort sine egne undersøkelser basert på ukjent kilde:
Aviation Herald har gjort sine egne undersøkelser basert på ukjent kilde:
On Jun 5th 2015 a source contacted The Aviation Herald indicating, that the aircraft had entered a full stall on a visual approach to Svolvaer's runway 19 with the captain being pilot flying. The aircraft was turning base when the airspeed sharply dropped and the stickshaker activated. The engines were accelerated to maximum power available, the pitch continued to increase until the aircraft entered full stall however and the captain basically froze. The first officer took control of the aircraft, pushed the nose down, managed to recover the aircraft from the stall and pulling +2.7G arrested the descent at 25 meters AGL. The aircraft subsequently diverted for a safe landing. Following the occurrence the captain provided a report about the occurrence to the safety department of the airline which prompted both engines to undergo checks for overtorque before the aircraft was returned to service. Our source said: "The captain drastically understated the severity of the situation. The AIBN cannot investigate what it does not know." The first officer left the company and joined another airline.